Announcement

Collapse
No announcement yet.

Dip in power after peak torque dyno

Collapse
X
 
  • Filter
  • Time
  • Show
Clear All
new posts

  • Dip in power after peak torque dyno

    Top dyno was a few days ago
    Second was last year
    A/F is solid, I'm wondering if it's ignition related, maybe I need to swap the plugs and wires, it dips at 4k and gets back on track at 4.5k. I think it's strange that it clears back up at 4,500 and is good all the way till 6k. Base timing is set to 10


    Interested in being a VIP member and donating to the site? Click here http://dfwmustangs.net/forums/payments.php

  • #2
    VTEC butterflies stuck?
    Originally posted by PGreenCobra
    I can't get over the fact that you get to go live the rest of your life, knowing that someone made a Halloween costume out of you. LMAO!!
    Originally posted by Trip McNeely
    Originally posted by dsrtuckteezy
    dont downshift!!
    Go do a whooly in front of a Peterbilt.

    Comment


    • #3
      Vtec was removed when i put the ecam in
      Interested in being a VIP member and donating to the site? Click here http://dfwmustangs.net/forums/payments.php

      Comment


      • #4
        Well there ya go.
        Originally posted by PGreenCobra
        I can't get over the fact that you get to go live the rest of your life, knowing that someone made a Halloween costume out of you. LMAO!!
        Originally posted by Trip McNeely
        Originally posted by dsrtuckteezy
        dont downshift!!
        Go do a whooly in front of a Peterbilt.

        Comment


        • #5
          I've seen similar issues on LT1 cars with opti issues, I wonder if it's the TFI module.
          Interested in being a VIP member and donating to the site? Click here http://dfwmustangs.net/forums/payments.php

          Comment


          • #6
            could be a fuel issue, no A/F on the graph so it hard to tell. Could be also over timed in that area, and could be getting into some pre-ignition around MBT.

            Comment


            • #7
              Originally posted by JETFAST View Post
              could be a fuel issue, no A/F on the graph so it hard to tell. Could be also over timed in that area, and could be getting into some pre-ignition around MBT.
              a/f looked pretty solid, timing is only 24 total on p's, but you made me think of the fact that the fuel in the tank was 4 months old, I wonder if that had anything to do with it.
              Interested in being a VIP member and donating to the site? Click here http://dfwmustangs.net/forums/payments.php

              Comment


              • #8
                very likely your issue. always test with fresh fuel. pre ignition and or detonation, usually looks real "wavey" like that threw the curve. Even with graph smoothing at it's greatest. Usually a cause of "riding" the knock sensor.

                Comment

                Working...
                X